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Date |
Event |
02/01/2005 5hrs Speedo Calibration
Exhaust manifold |
This is cumulative time over Christmas and
the new year while I have manoeuvred the car to determine the circumference
of loaded tyres, tests and measurements to calculate the data required
to calibrate the speedometer. The quote for Cermakrome finish for the
exhaust is over £250. I've started to clean up the exhaust manifold,
painted it with Kurust and will treat with high temperature paint for the
time being. I've also got to work on getting the studs replaced where the
down pipe mounts before I paint the manifold.
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03/01/2005 5hrs Rear Body shell |
Some time back when I was fitting the boot
lid, I noticed that the bottom of the boot lid was not parallel with the
rear chassis cross member. I suspected that it was because the rear body
shell was not sitting square in the chassis. I had spoken to Chris
Bowyer about it. Nostalgia do not pay much attention too the dimensions
given in the build manual drawing but prefer to check the rear of the body
alignment by eye. Standing from behind the vehicle if it looks right then
that will do. It is hard for me to do that, in the confines of my
garage. I had been very careful during the fitting of the rear body shell to
check and recheck the measurements and to get the body ( as I thought)
square on the chassis. However last week when the vehicle was outside for
calibration of the speedometer. I took a good look from behind. Again it was
hard to tell since the driveway sloped away to the right. It didn't look too
bad but I was still bothered by the bottom of the boot lid not being
parallel to the chassis. Today I decided to see if I could correct it. I
removed the rear offside wing and unbolted the body shell. It was also
necessary to loosen the boot lid but I keep it in place to aid alignment.
I slotted the body mounting holes on the RHS and moved the body up slightly.
I trimmed the sides of the boot lid at the bottom, correspondingly trimming
the boot lid aperture to improve the fit. I ended the day putting it
all back together again but still have to secure the boot lid again before I
can tell if I have improved it.
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04/01/2005 4hrs Exhaust manifold |
The exhaust manifolds, as removed from the
XJ6, had 2 bolts and 2 studs securing the down pipe to them. I'm pretty sure
it is supposed to have 4 studs. I attempted to remove the existing
studs the other day but could not get enough heat in to the manifold to help
shift them. I spoke to John Hopkins yesterday about this and he agreed
to help to get them out using a stud extractor and his propane torch.
I turned up at his place this afternoon armed with both manifolds and 8 x
3/8" UNF bolts to turn in to new studs. John's propane torch was much
more powerful than mine and we soon had plenty of heat in to the manifold.
Using a 10mm stud extractor we attempted to remove the studs. Despite being
careful we managed to snap 3 of the studs and extract one. Then it was
a long haul of drilling out the centre of the broken studs and attempt to
extract them with an "Easiout" I've never had much success with "Easiouts"
and so it proved. Plan "B" was to drill out the centre of the studs
until we could just see the threads ,then break the thread out with a small
chisel or a scribe. Even with the largest drill we could safely use,
we could still not see enough of the threads to break them out. We ended up
using diamond grinders fitted to a Dremel to finish opening out the holes
until the threads were just visible. Then we used a 3/8" UNF plug tap
carefully inserted in to the threads to make sure we did not cut a new
thread but clear out any old thread and corrosion. The end
product was perfect new threads that looked better than the originals.
John is going to make the new studs tomorrow.
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05/01/2005 2hrs
Boot Bridge
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Adjusted the boot lid bridge and hinges.
Painted the fuel tank and the front rear wing stays with undercoat. |
10/01/2005 6hrs fuel Tank Exhaust Manifilds Front Dumb Irons |
I may have said in the past that I am not a
fan of unpainted aluminium. I know it does not corrode in the accepted sense
that steel rusts but it does oxidise. This is my reasoning for painting the
fuel tank. it is out of sight and out of mind but with a good coat of paint
it is protected from salt, and wet. I finished painting it with
Hammerite Smooth Black paint today. Yesterday I cleaned and painted the new
exhaust down pipe curing the rust, which had already started to form, with
wire wool and Kurust paint. I finished it off with 2 coats of Silver very
high temperature paint. Today, I got the exhaust manifolds and
the new studs back from John Hopkins. The Manifolds I degreased with
Hammerite Paint Cleaner and painted the manifolds again with Kurust.
While I was waiting for them to dry I started work on fitting the front dumb
irons. These brackets are used to mount the front bumpers. They mount on to
the front body - chassis mounts (fitted when the front body was
fitted). The outboard attachment points have to be drilled in the body and
then attached to the body / chassis stays. I began by jacking up the
front RHS of the chassis, checking it with a level to compensate for the
slope on my garage floor. This was a precaution to ensure that I got the
dumb irons mounted straight and level with the chassis and the body.
With the dumb irons mounted on the inboard mounts and tightened up
sufficiently to hold them in place but their positions could still be
adjusted. I placed a long spirit level across the top of them to get them in
to line and level. I had put masking tape behind the dumb irons where
the outboard mounting points should be and marked the position of the
brackets with a pencil. I was going to mark the position outboard mounting
hole through the dumb iron on to the body when I realised that the hole
would be spaced away from the body when finally mounted and thus position of
the hole would move. I stopped at this point to consider the best way
of accurately finding the position for the hole.
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12/01/2005 2hs Fuel Tank Exhaust Manifold Battery |
Not much to show for my day off. I was
planning to get the fuel tank, the exhaust manifolds and front dumb irons
fitted. I was getting ready to fit the tank when I noticed the paint
on the sides of the tank was a bit thin. So I had to give them another coat.
the paint seemed slow to dry today and I wanted to be sure that it was
hard before I fitted the tank which meant that I had to abandon fitting it.
I did manage to get the exhaust manifolds fitted. I fitted a couple of
new studs in the block and greased them with copper slip. I fitted the new
studs that John Hopkins had made for me to the flanges again lubricating
them with copper slip. Then it was fit new gaskets to the block and secure
the manifolds top the block with new plain washers, spring washers and new
brass nuts. It will probably need tightening with a torque wrench, before
the engine is run. I got a new battery from Halfords today having used
the previous one on the Land Rover after its battery died last week.
It was just a happy coincidence that the "120" and the Land Rover use
the same battery.
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13/01/2005 2hrs
Fuel Sender Access Panel
Bonnet
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I had one of my support phone calls to
Nostalgia today to clear up the purpose, shape and size of the access hole
to be cut in the inside rear wing panel. It is to facilitate changing
of the fuel tank sender if it were ever to be necessary. Secondly to discuss
the details of marking and cutting the outer hole for the front dumb irons.
The factory mark the hole immediately behind and straight through the
dumb iron on to the bodywork. Then open out the hole to 25mm to accommodate
the chrome mounting rod. I rechecked the position of the dumb irons to
ensure they were straight and level. I marked the position of the holes
using a length of studding dipped in engineers blue and inserted through the
dumb iron.
I had been unhappy with the fit and position
of the bonnet ever since I first fitted it. Whilst I was talking to the
factory I discussed it with Chris Boyer. During the
conversation I described the position and the fact that the bonnet appeared
too wide and too high at the back next to the scuttle. We realised
that the bonnet was too high and that the position of the hinges on the
bulkhead was the problem. The factory further elongate the holes in
the bulkhead downwards to lower the hinges which should fix my problem.
I took the bonnet off to fix the hinge
problem. This was no hardship because I realised it would have been better
to have fitted the exhaust manifold and the down pipe before the bonnet was
fitted. Whilst the bonnet was off I took the opportunity to fit the
down pipe. It was still a fiddly job for one person but much easier without
the bonnet.
|
15/01/2005 4hrs
Bonnet |
I removed the bonnet hinges and by a
combination of a cutter fitted to the Dremel and a round file I elongated
the slots in the bulkhead about ¼" downwards. This enables the hinges to fit
lower. I repainted the bulkhead to cover up any scratches and the bare
metal edges of the slots. Whist I was waiting for the paint to dry I
returned to the fitting of the dumb irons. I rechecked the position of
the dumb irons with a long spirit level to ensure they were straight and
aligned across the front of the car. Using the marks I had made
earlier as a guide I drilled the body through the dumb irons at the
centre of the hole in the dumb iron. Lowering the dumb Irons out of
the way I drilled a 25mm hole centred on the pilot hole. I fitted the
chrome mounts and the body washers springing the dumb Irons in to place. I
lightly secured the dumb irons and the mounts in place and rechecked the
dumb iron positions. It was necessary to adjust them upwards slightly by
shaping the upper part of the 25mm hole woth a half round file.
|
16/01/2005
4hrs
Bonnet |
The paint on the bulkhead was now dry and I
refitted the bonnet hinges. Whilst I had the bonnet off I decided it
would be easier to fit the heater connections to the engine. I found
that the heater hoses from the XJ6 were in good condition and with a little
modification could be used. I cut one of the hoses to give me a right
angled connection. I then made up and adapter pipe from 15 mm copper pipe
and 2 right angled solder plumbing fittings, to connect between the
lower hose at the back of the engine block and rubber right angle hose.
The adapter pipe was cleaned and painted with etching primer and left to
dry.
I spent some time examining the fit of the
front wing stays. According to Nostalgia these stays will need to be tweaked
to get them to get and to ensure they do not put a strain on the body.
Nostalgia is right they will need adjusting but I can not decide exactly the
best lace or angle to bend them to get them to fit. they are pretty
substantial to bend and I decided to sleep on the problem and take another
look at it tomorrow.
I ended up trial fitting the bonnet now that
the hinges are lower. The bonnet is a better fit and there is plenty
of room between the underside of the bonnet and the hinges. I'll
finish the cooling system tomorrow and then refit the bonnet.
|
17/01/2005
2hrs Rear Wing StaysFuel
Tank Sender |
Refitted the front stays to the
rear wings. Painted the heater pipe, satin black, and left to dry.
Checked the fitting instruction fro the fuel tank sender. I measured
the depth of the tank. This is required to work out the length of the arm
for the float. As usual the depth of the tank 320 mm was not an
exact match to the data in the instructions. The advice given is to choose
the number closest and set the arm correspondingly. I plotted the data
in to Excel. The relationship between depth of the tank and the length
of the arm turned out to be a straight line. This enabled me to work out the
equation and determine the exact length of the arm 176 mm. It probably
makes no discernable difference to the accuracy of the fuel gauge, whether
the figure in he table is used or my calculated value. However I've decided
to go with my value.
|
18/01/2005 1hr Heater |
Removed the bonnet and fitted the hoses and
the pipes between the engine and the heater. |
19/01/2005 4hrs Fuel Tank Sender |
Today seemed to flash by and I have little to
show for it. I started by recalculating the length of the float arm
fro the fuel tank sender. I decided to work correct to the
nearest whole number, which worked out to be 177mm. I cut the wire of the
arm and the float to give maximum overlap. I cleaned the wires with
fine wet and dry then fitted the retaining clips and re-measured the length.
I clamped the wires together using a needle nosed pair if pliers held closed
with an elastic band round the handles. Rechecked the length again and
soldered the retaining clips in place. You need a fairly big soldering
iron in order to heat up the wires quickly and locally to prevent
overheating by prolonged application of the soldering iron during the
process. I used a 65W soldering iron. I then fitted the float to the
end of the arm and made one final check of the length. I covered
the gasket with a thin bead of h "Hylomar Blue" on both sides. The sender
was fed in to the tank via the hole in the side ,making sure the sender was
the right way up and the gasket aligned with the holes in the securing
plate. The tank was already fitted with M5 rivnuts . The sender was secured
to the tank with 6 x M5 x 15mm bolts , plain and "shake proof" washers.
finally I fitted two strips of close cell foam rubber to the mounting
flanges of the tank to act as a gasket.
During a break in the proceedings this
afternoon I contacted speedy cables to enquire why I had not had a response
to my e-mail of last week . I got a reply within the hour with a quotation
for refurbishing the instruments from the XJ6.
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22/01/2005 4hrs Fuel Tank fitting |
I cut the holes in the cell foam gasket for
the tank mounting bolts, then set about mounting the tank. Mounting
the fuel tank is really a two man job but it can be done single handed.
the tank is fed up from underneath the car. I find the best way was to feed
the top of the tank up and past the boot hinge bridge and the slide the
bottom in to position. Take care not to catch the fuel gauge
transmitter on the fuel tank mounting rail. What is needed now is to
hold the tank and the support bar in position whilst feeding in the mounting
bolts and loosely tightening up the nuts. This is still awkward but
achievable with two people. If like me you are on your own the following
will work. Make 2 wooden supports for the tank from 2 x 8"
pieces of wooden batten (2x1 will do) and 4 x 2" pieces of (4"x 2")
Screw a piece of the 2"x 4"x2" to end of 8" batten. These act as
supports for the tank and loosely bridge the support bar whilst it is
located and bolted in place. I placed 6 breeze blocks (3 each side)
under car. I placed 2 bottle jacks (1 each side on top of the breeze
blocks). The wooden tank supports were placed on top of the jacks,
then raised under the tank by adjusting the bottle jacks until they were
supporting the tank in position. the mounting bolts were loosely
inserted and tightened finger tight. The bottle jacks were lowered so that
the mounting bolts took the weight of the tank. The support bar was
now placed across the wooden mounting supports and the bottle jacks raised
again to support the tank. Because the wooden supports are deeper than
the support bar the tank is supported but the bar can be moved at=round
quite easily. The mount bolts were removed and the tank support bar offered
up in to position The mounting bolts were reinserted and tightened up
finger tight again. The wooden supports, bottle jacks and breeze
blocks were removed. The tank and the support bar remaining in place.
It was then a simple matter of fully tightening the mounting bolts.
|
23/01/2005 4hrs Bonnet |
It was time to put the bonnet back on today
after my fitting of the exhaust and extending the hinge mounting slots in
ht34 bulkhead. It was a fiddly job the first time around but I seemed
to be having exceptional difficulties aligning the hinges with the holes in
the bonnet. Eventually I took the bonnet off again and removed the hinges
from the bulkhead. Fitted the hinges to the bonnet just about finger tight.
I Replaced the bonnet, with the hinges fitted, on to he bodywork aligning it
centrally and pushed as far back as it will naturally go. I
fitted the top hinge bolts to the bulkhead by reaching through
the scuttle in to the engine bay. The bolts are secured with penny
washers. spring washers and plain nuts on the inside by reaching up through
the cut outs in the underside of the bulkhead. Tightened the bolts
finger tight and rechecked the alignment of the bonnet. Final
securing of the hinges is a two person job, I will do this tomorrow.
|
28/01/2005 2hrs Bonnet Instuments |
This is all the time I've managed to find to
spend on the car as the domestic chores of helping my daughter and son in
law move house has demanded much of my time. I've put the bonnet on
and secured the hinges to the bonnet. Securing the hinges to the bulkhead
has still to be done. I've worked what to do about the instruments
from the XJ6. I've sent the Speedometer and the Tachometer for refurbishing
and ordered replacement Fuel, Oil Pressure, Water Temperature and voltmeter
gauges. The cost of refurbishing the smaller instruments was about £2.00
dearer per instrument than buying new ones. I sent the order and the
instruments off to day. I also dismantled the XJ6 dash board and
cut the instrument console out of it. This can be used as the central
dash panel and I have salvaged it in case I decide to use it and not
make a new one.
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Total
Number of Hours this Month = 51 hrs |
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Total Number of hours to date
= 946 hrs |
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